So I set about with a plan. Take some parts of the OE spring packs to me a zero rate spring. Just adds height, no capacity or rate change.
New springs (V2) correct length this time, but no lift. My god are they heavy.
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So after they were installed, we figured out they provided no lift. So I came up with a plan. Use the block and the anti wrap leaf from the OE pack to get some height.
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The OE Springs got broken down giving me ~1.25″ of lift height.
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Then came the fun of trying to jack up a big heavy truck, in my gravel driveway… (I had paid to have springs installed twice already, I had to DIY this time). Luckily my neighbor had a big pile of 4×4 chunks of various projects, so I was able to make cribbing to hold the truck up. It had to be held from the frame so I could remove the axle from the springs. The plan was to remove the Ubolts, lift the truck off the axle so I could roll it out of the way, install the new spring parts and the put the axle back.
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Got one side in the air, Ubolts removed, and went to roll the axle out of the way. That’s when I was reminded I have a limited slip rear end. Can’t roll one side….. Enter ratchet straps, webbing a second jack and cursing.
I was able to just get it forward enough to get the center pins out. Once they were out I went to slip the parts in and the new center pins would not fit. The spring builder used a smaller pin than Ford. I had to drill through the entire spring pack for the larger centering pin. But it worked, and we got the new old bits in place.
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Then it was just reverse procedure to get the axle back to the correct place and lower the truck down onto it. Then repeat on the other side. Longer U bolts were made for both sides and we took it out the following weekend. Much better ride, still not much lift after it all settled in.